![]() |
Deep Sigh
https://cimg5.ibsrv.net/gimg/bikefor...cd477cfdac.jpg
Finished the 3 month Centurion Prestige build. Adjusted everything on the stand. Test rode up and down the block, brifters and brakes, it's working nicely so I go to end of the block, turn left uphill and stand on the pedals. I didn't finish the second rotation when it came apart violently. This was a tough lesson; when building on an old frame with unknown history, build and test before any cosmetic work. Only 10 minutes to live https://cimg0.ibsrv.net/gimg/bikefor...e7433ae5c0.jpg So, the worst has happened; n-1, and this will be rectified soon! |
What a shock!
|
Ugh. I feel your pain! I've never seen a failure like that. I wonder what kind of forces, and in what direction(s), caused such a failure.
|
Get it fixed. It will be worth it.
|
Holy crap, never seen that before. Hopefully you came out of it unscathed.
|
Originally Posted by smd4
(Post 22449389)
Ugh. I feel your pain! I've never seen a failure like that. I wonder what kind of forces, and in what direction(s), caused such a failure.
|
Originally Posted by Bad Lag
(Post 22449396)
Get it fixed. It will be worth it.
|
Originally Posted by SurferRosa
(Post 22449406)
Nah. What happened there is an anomaly.
|
Awful... Though the half a dropout is proof positive of the enormous wattage that you clearly put out. If it were mine, I'd hang it on the wall and recount the story to houseguests. Good luck finding your n+1!
|
Originally Posted by BTinNYC
(Post 22449401)
My guess is the dropout had been bent back and forth in its life and was weakened at the thinnest section, at the threaded hole.
|
Originally Posted by smd4
(Post 22449443)
I would think the force exerted would tend to pull the axle towards the front of the dropout, along the slot. What caused it to force the bottom part of the dropout (I'm guessing), down, vertically?
|
That build came out pretty nifty. Sorry that happened.
|
Well, all the old books say that a great benefit of steel frames is that they can be relatively easily/cheaply repaired. Time to place that ancient wisdom into practice!
|
Originally Posted by jrg1244
(Post 22449435)
Awful... Though the half a dropout is proof positive of the enormous wattage that you clearly put out. If it were mine, I'd hang it on the wall and recount the story to houseguests. Good luck finding your n+1!
2. Worth fixing. 3. Take the picture, frame it, mount that on the wall as proof of your wattage. 4. Refine the story to generate swoonage. |
Long drive, but...
Come to Harvard and I'll MIG it for you. Bring a nice Calvados or green chartreuse and be prepared for an evening of fun. My prior dropout work is here. I'm confident I can do this. Super easy, especially if you can forego the adjuster. I can redrill and tap the adjuster as well, just a bit more work. ;) |
Originally Posted by scarlson
(Post 22450021)
Long drive, but...
Come to Harvard and I'll MIG it for you. Bring a nice Calvados or green chartreuse and be prepared for an evening of fun. My prior dropout work is here. I'm confident I can do this. Super easy, especially if you can forego the adjuster. I can redrill and tap the adjuster as well, just a bit more work. ;) |
Originally Posted by BTinNYC
(Post 22450030)
You would weld the two parts together?
I'd rather do that than try to source another dropout, melt and grind and file the old one out, prep everything, and braze it. The bottom of the dropout doesn't see much stress. This is way easier than the one I just did, linked to above. Only risky thing is trying to drill through the weld and tapping that hole for the adjuster. Much easier and stronger if you forego the adjuster on that side. But I can drill it too, if you must. |
This is the one argument in favor of stamped dropouts over forged.
It is also possible that the dropouts were not properly aligned, or that the previous owner had broken a rear axle and stressed the drive side dropout in the process. |
Originally Posted by jrg1244
(Post 22449435)
Awful... Though the half a dropout is proof positive of the enormous wattage that you clearly put out. If it were mine, I'd hang it on the wall and recount the story to houseguests. !
|
Any signs of corrosion in the threads of the adjuster hole? Just grasping at straws here.
That's gonna be a pretty build once it's back together. |
Originally Posted by scarlson
(Post 22450041)
Sure I would. For a bottle of green chartreuse and some agreeable company. Would also consider aņejo mezcal or tequila...
|
Originally Posted by plonz
(Post 22450260)
Sam, a welder and tequila... what could possibly go wrong!
Good one ! :roflmao: |
Originally Posted by smd4
(Post 22449389)
Ugh. I feel your pain! I've never seen a failure like that. I wonder what kind of forces, and in what direction(s), caused such a failure.
|
Originally Posted by nomadmax
(Post 22450285)
I've seen that before. In those cases, it was from putting a longer OLD axle in frame designed for 120/126mm without cold setting and making sure the dropout faces were parallel to each other. Mind you, that's not what I'm saying is the case here.
I will very closely check the DOs after fixing. I did not successfully cold set because the stays were like spring steel (wouldn't hold a mm of bend, even after spreading to 165mm, yet relatively easy to spread by hand) and now my check for parallel with a homemade tool feels cursory. Edit PS Wouldn't that misalignment become evident while setting up the RD? |
I'd get that MIG or TIG welded for sure. As said, welding would fill in the tapped hole, but it could be drilled out and tapped after. If MIT is too far, maybe someone at RPI?
|
| All times are GMT -6. The time now is 04:00 PM. |
Copyright © 2026 MH Sub I, LLC dba Internet Brands. All rights reserved. Use of this site indicates your consent to the Terms of Use.